Headed out to the garage tonight all ready to pull one of the carbs and clean it within an inch of its life. I decided I'd start with the mag side and pulled the choke cable. Thats when I noticed how little slack there was in the choke cable which prompted me to remember how the choke lever had felt weird yesterday. I pulled the other cable and it seemed short too. I followed the cables back to the lever and found the back had popped off and pulled back on strangely so the choke was always half engaged. Got that re-arranged, got the cables back in place, fired the sled up and it still ran like crap. For some reason I kept it running and after maybe a minute it make a little noise and idled perfectly!
I think that yesterday in running with the choke on I'd loaded some gas into the bottom end of the engine and what I saw today was that burning off and once it did the sled running right. It was late when I started so I didn't want to run the sled too much, make a bunch of noise and piss off my neighbors but I'm pretty pleased.
Unfortunately I noticed the headlight is out, I put my trouble light on the line to the seat and it lit up so either the bulb is burnt out or disconnected. I wouldn't be surprised if its burnt out.
Anyway I decided that since the carbs don't have to come off (probably) I'd put the seat on. That was an exercise in frustration. Here's a free hint that I should have already learned from farting around with the Ski-Doo, test fit the plywood before attaching it to the seat. I didn't make the cutout at the front deep enough or wide enough. Now I need to take the seat apart again, recut the base and reattach. I'll definitely trial fit the base before I reattach the foam though!
Anyway, getting closer, nearly there!
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